When the pilot of the new, kit-built airplane realized he had lost throttle control, he decided to land at the home field of the manufacturer. He shut down the engine in the landing pattern, but miscalculated the power off descent rate, and landed short of his intended landing runway. Subsequent examination of the engine by factory personnel revealed that a castellated nut securing the cockpit throttle cable linkage to a threaded connection on the fuel metering shaft of the fuel servo had backed off due to a missing cotter pin. This allowed the linkage to disconnect and resultant loss of cockpit engine power control.

| FAA | NTSB Final | News |


Posted By: Brett Ferrell
Friday July 17th, 1998 at 7:26 PM

Categories: Accidents
Tags: 1998 Accident FL Hyde N96HV Non-Fatal RG SE Sebastian Velocity

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